I plugged her in and left the mini-splits set as low as I could (60 degrees F). Amazingly with temperatures dipping into single digits, the system could still extract heat from the ambient temperatures. I thought I had enough heat in the utility bay to prevent freezing, but after a couple of below zero nights, one of the plastic PEX manifolds burst. I also had the refrigerator to repair and I decided to send the Victron back for a go-over since it was still under warranty. I was convinced the inverter was the cause of the refrigerator cable fire.
So, my first project in the Spring was to pull the inverter and send it in for testing. The good news was that there was nothing wrong with it. The bad news was there was nothing wrong with it. I'm still unsure of the cause of the meltdown. I got the inverter back and re-installed it with a few "better ideas" added. I can't find any abnormalities in the system. I hate it when that happens!
Donor accelerator pedal |
The first step was to remove the system from the parts bus. That was pretty straight forward - unbolt the accelerator pedal assembly up front and the piston assembly in back on the governor. The pedal assembly is a proportional air valve with three air lines. A supply line from the front air tank, a distribution line to the actuator piston on the governor, and a vent line to depressurize the air valve. The picture shows the valve with the pedal removed.
The old pedal had to be cut out from the brake/accelerator assembly and replaced with the air pedal mechanism. It looks easy. Took about two hours.
The old pedal had to be cut out from the brake/accelerator assembly and replaced with the air pedal mechanism. It looks easy. Took about two hours.
New pedal |
Old accelerator pedal |
Next, the old cable throttle was removed. Then the air throttle had to be modified because the governor on the Bus was different than the donor's. The mounting plate had to be modified by adding an extension plate and the pivot return arm flipped to make it work on my governor.
New air throttle |
Old cable throttle |
I ran 45' of 3/8" air hose from the pedal assembly to the throttle piston, aired up the system with the shop compressor, fired up the Detroit, and volia! Great throttle response, and a drastic improvement in overall drivability. I don't use the clutch once rolling, so quicker shifts are possible since the engine revs drop quicker with the air throttle.
STILL TOO HOT
The coolers are hung with rubber hangers stacked one behind the other. A remote, 12v electric, gear driven oil pump moves 5 gal. per minute from the bottom of the oil pan, through the oil coolers and returns the oil via a fitting in the block below the oil fill. I cut a hole in the bay door and also in the aluminum panel separating the compartment from the area behind where the coolers are
located. I mounted a Flexalite fan to push air through the coolers. I've done a short run, but not under conditions that would put the system to the test.
Next: The Shop
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