WEATHER
BASED WORK SCHEDULE
Winter
in Michigan has gotten really weird. We never get deep snow like in
the old days. Two weeks ago highs were in the teens, then up into
the fifties, then down to six below, then up to sixty two. This week
it's ranged from 55 to10 – crazy! So – the conversion process
has become closely linked to the weather. On warm days I tackle
“outside” projects. On really cold days I retreat to my heated
shop and work there. Heating The Bus is a third option but not very
efficient yet, so it's limited to the 30 to 40 degree days. I'm
close to installing the propane furnace for The Bus which will
improve that situation. But, for now, I work where the weather
dictates. The last 65 degree day I installed all the outside marker
lights and new engine sending units. I'm just finishing up linking
all the marker wires. There are 16 marker lights in all. I don't
have the original triple lights on the roof restored yet, so for now
I'm using 2” round plug-ins. I can use the same plugs for the
bulbs in the original triple housings, but they won't go back on The
Bus until after it's painted.
Here's
the new driver's panel in the process of rewire. The main ON/OFF
switch on the dash controls a relay that powers a fuse block to all
circuits that need to be on when The Bus is underway (fuel valve,
high idle, starter solenoid, reverse solenoid, cooling fans, etc.).
A second fuse block has constant power for circuits like marker
lights, flashers, headlights, propane furnace, etc. The original GM
wiring also had a “fail-safe” circuit that monitored oil
pressure, water temperature, and some other stuff I can't remember.
It would would shut the engine down automatically if parameters were
out of bounds (apparently they thought the driver was too stupid to
count on watching his gauges). The problem with this is that if any
component (sensor, sending unit, relay, fuse, connector, ground,
etc.) in the circuit fails and shuts the engine down, tracing the
failure could take forever. I'm opting for watching the gauges on my
own and not replacing this circuit. The really crazy thing about the
original circuit is that it had and OVERRIDE switch! So if there
was no oil pressure the driver (AKA idiot) could hold the override
down, restart the engine and drive it 'til it seized up. Great idea!
![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEiA1XVqqBZoDsUE5bSx_iMv86Oh3iz-QKOhDDnubdlnHAOXItYUFUNmJeyr8XY_jiPb3xlHDtWcdOahmm7r5lgPd3RdHbXtuC0gLutbskSn0vSJGV2ZzsZf49sn0uno6P2ATX1JZNS808k/s400/FULL+VIEW.jpg)
I drew
up the ceiling console grill on a CAD program and took it down to my
water jet cutter guy. Greg Ahrens (http://www.mfg.com/Manufacturers/National-Waterjet-1205690_en.html). We cut three pieces out of 3/16th
aluminum 84” x 16”. My plan was to back-light the grill with
mini fluorescents, but I wanted to keep the ceiling as high as
possible, so I decided on LED rope which is only 5/8th
inch diameter. The other option was LED adhesive strips, but they
cost about $150 for 16 feet. I needed 150 feet! That's almost
$1500! I bought a single 150' rope for $150.
I taped them up on the ceiling in six rows to see if it would provide sufficient light. It works great! It lights up The Bus like Times Square on New Years Eve or the Superbowl at the start of the second half!
I taped them up on the ceiling in six rows to see if it would provide sufficient light. It works great! It lights up The Bus like Times Square on New Years Eve or the Superbowl at the start of the second half!
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