As
you may already know from some facebook posts, I came down with
mysterious muscle/tendon pain that felt like I had worked out at the
gym for 12 hours after being a couch potato for decades. Morning
pain and stiffness was so bad that I was unable to reach over
shoulder height, couldn't lift my knees to my waist, couldn't squat
and get back up, couldn't ride my mountain bike, and had lost 90% of
my grip due to pain in my wrists. It took three months to get a
diagnosis and start treatment. Needless to say, not much got done
with the bus. I have polymyositis rheumatica (PMR) – an auto-imune
disease similar to (but not as bad as) rheumatoid arthritis, lupus,
scleroderma, etc. Notice that this is only one letter away from PMS,
a much more horrible condition. I started taking Prednisone two
weeks ago, and I'm now back 100%. Amazing! I'll have to be on the
Prednisone for 6-12 months. It has nasty side effects, but with a
healthy diet and regular exercise, I should be able to keep them to a
minimum.
We went to the bus rally in Flint and also to the Woodward Dream Cruise a few weeks ago. Learned a lot and took home a lot of great ideas. There were 31 bus conversion there.
We also did the Woodward Dream Cruise. 40,000 customs and restorations cruising down Woodward Ave. and they estimated over 1 million spectators.
We went to the bus rally in Flint and also to the Woodward Dream Cruise a few weeks ago. Learned a lot and took home a lot of great ideas. There were 31 bus conversion there.
We also did the Woodward Dream Cruise. 40,000 customs and restorations cruising down Woodward Ave. and they estimated over 1 million spectators.
My
brother, Todd, has been over through the Labor Day weekend –
actually from Saturday through Wednesday. We reached a long sought
milestone on Tuesday. We finished laying the structural floor which
gives the bus about 50% of its rigidity. This took way longer than I
expected – following what I call the “5X Rule”. The 5X Rule
only applies to something you've never done before - versus the “2X
Rule” which is the actual time to complete a project you've done a
few times before – versus the “1X Rule” which applies to stuff
you've done ten times or more. All together I laid nine sheets of
plywood and only averaged 0.75 sheets per day. That's twelve full
days (8-10 hrs.) to lay nine sheets. The top of all the bulkheads
had to be rotary sanded with 80 grit to get good glue adhesion. Each
piece had to be rabitted at the side wall to slide under the bus
rails running down the sides. Then all contact surfaces with the bus
frame and plywood edges were glued (twenty four 10.5 oz. Tubes of
liquid nails). I used an air powered glue gun. Finally, the sheet
was drilled and screwed down with ¼” self-tapping flat-head Torx
bolts. I used about 500 bolts, not counting the edges, which
requires nuts and bolts every four inches – about another 100
bolts. This part is a two man job requiring one person inside the
bus and the second under the floor on the outside. The final sheet
was dead on square!
I've
also been stripping the paint off the outside. This is a slow
process because you have to wait 8-12 hours between application of
the stripper and removal. The stripper I'm using is called
Aqua-Strip and is very nice to work with. It's like thick wallpaper
paste. It doesn't run, is non-toxic, and cuts through the paint
well. The only negative - $78.00 a gallon! I figure it will take 5
gallons to strip the whole bus. It has taken three applications to
remove the six layers of paint down to pristine aluminum. The OEM
green base primer and gray second primer were very good products.
They're very thin coats, but require a fresh layer of stripper and
steel wool to remove. We've got about 1/3 of the bus down to
pristine aluminum.
On
the mechanical side, I've got the radiator out and have modified (as
in torn out crap to make room) the engine compartment to get the
radiator up further from the road. As it hangs out behind the rear
wheels it was prone to skid damage on slanted transitions from
parking lots, etc. to the road. This will require rerouting all the
coolant plumbing at the front of the engine. I ordered four 1200 cfm
electric fans to pull air through the radiator. They might arrive
tomorrow (I hope, I hope). I'll have to custom fabricate a radiator
shroud to enclose the fans to get maximum air flow through the
radiator.
With
the help of Kevin VanVeelen (my expert glass man) we have installed
and removed the windshield twice, so far. The windshield is two
piece with a bar down the center. I want to eliminate the bar to
give a smoother look to the front of the bus, and eliminate the
annoying obstruction of the 1” wide center bar. On first attempt,
we could not get the center edges of the glass close enough to meet
in the center without being too far from the outside edges – even
with the center gasket still attached. That process took us six
hours as the gasket has what's called a locking strip that you press
in with a flat plastic stick and lots of soapy water. Once convinced
the windshield would not be water tight, we pulled the locking strip
out (3 min.) and came back a second day for another shot. This time,
after welding a 3/8” wide aluminum strip to the outside edges of
the window opening, we tried again. Still too big a gap in the
center. This time it only took us three hours to get the glass in
and out! Now I have a plan to use panel adhesive and one and a half
inch wide aluminum to narrow the windshield opening. We'll have to
shorten the original gasket, but I think it will work this time.
I've
got the driver's seat positioned, so we can go shopping for seats.
Becky, Teri and I went to Ikea and discovered that I can do all the
cabinets and LED lighting using their products. This will mean a
huge time savings in building cabinets and installing lighting.
I
hope to get plates, and have her on the road in a month or two. The
inside will be empty, but I need to keep the mechanicals operational
and get some shifting practice in. Hope you enjoyed this issue of
This Old Bus.
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